通化硕抠家具有限公司

    304L連鑄圓坯的連鑄工藝優(yōu)化及穿孔性能提高

    Optimization of Casting Process for and Improvement of Piercing Performance of 304L CC Round Billet

    • 摘要: 選取中包鋼水過(guò)熱度、二冷段比水量、二冷段電磁攪拌電流以及拉速4個(gè)工藝參數(shù)進(jìn)行正交試驗(yàn),分析不同條件下304L連鑄圓坯段樣和片樣的中心縮孔及裂紋情況,確定連鑄工藝參數(shù)的最佳組合,并從不同角度分析連鑄圓坯中心縮孔及裂紋的產(chǎn)生原因。實(shí)際穿孔制管結(jié)果表明:縮孔及裂紋良好的連鑄圓坯具有較好的穿孔性能;當(dāng)片樣縮孔及裂紋均在0.5級(jí),段樣縮孔寬度≤7.5 mm,大于3 mm的縮孔長(zhǎng)度與試樣長(zhǎng)度的比值≤24.91%,可保證連鑄圓坯具有良好的穿孔性能。

       

      Abstract: An orthogonal test is conducted with the four major process parameters, i.e., the superheat degree of molten steel in the tundish, the water ratio of the second cooling section, the current for electromagnetic stirring(EMS), and the withdrawing speed so as to analyze the central shrinkage and crack as stay with the sectional and sliced samples of the 304L CC round billet under different conditions, and thus to determine the optimal combination of the CC process parameters.And the causes for occurrence of the central shrinkage and the crack are analyzed from different perspectives.Result of actual piercing operation shows that the CC round billet with highly acceptable shrinkage and crack presents good piercing performance, and that provided that the shrinkage and crack of the sliced sample are both classified as Class 0.5, and for the sectional sample, its shrinkage width is ≤ 7.5 mm, the proportional of the shrinkage length >3 mm to the sectional sample length is ≤ 24.91%, it will be ensured that the CC round billet possesses excellent piercing performance.

       

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