通化硕抠家具有限公司

    伺服控制技術(shù)在噴碼機設(shè)備中的應(yīng)用

    Application of Servo Control Technology to Code-stenciling Machine

    • 摘要: 針對噴碼機早期設(shè)備沒有自動識別糾偏系統(tǒng),每次更換鋼管規(guī)格調(diào)整機器人的運動軌跡或在機器人的噴印過程,經(jīng)常會出現(xiàn)損壞噴頭等噴印設(shè)備部件的問題,在原噴碼機機器人前臂增加伺服控制升降機構(gòu),將原來安裝在機器人前臂的噴頭等噴印部件安裝到升降機構(gòu)。在調(diào)整機器人運動軌跡或噴印過程中,該伺服控制系統(tǒng)通過檢測噴頭與鋼管內(nèi)、外壁的距離,自動控制噴頭機構(gòu)升降,始終保證噴頭與鋼管內(nèi)、外壁的距離處在設(shè)定數(shù)值范圍,從而避免了機構(gòu)與鋼管內(nèi)外壁碰撞,實現(xiàn)了噴碼機設(shè)備的高效智能、安全平穩(wěn)運行。

       

      Abstract: Addressing the problem that since the early-developed code-stenciling machine has no automatic identification-correction system,and thus each time when adjusting the robot movement track as per steel pipe size change or during the robot code-stenciling process,some components like the jet are frequently damaged,it is proposed to add a servo control lifting mechanism onto the front arm of the original code-stenciling robot,and accordingly the stenciling parts like the jet as originally mounted on the said front arm are now removed onto the lifting mechanism. Thus when adjusting the robot movement track or during robot code-stenciling process,the servo control system is capable of checking the distances between the jet and the inner surface and the outer surface of the pipe to automatically control the lifting-lowering of the jet device so as to get the said distances within the set value range. As a result it is avoided to have the mechanism knocking against the outer or inner surface of the pipe,which brings about the high-efficient,intelligent,and safe and smooth running of the code-stenciling machine.

       

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