通化硕抠家具有限公司

    T91毛管穿孔工藝的研究

    Study on Piercing Process for T91 Steel Pipe

    • 摘要: 針對(duì)熱軋穿孔T91管坯生產(chǎn)過程中產(chǎn)生的頂頭耗損嚴(yán)重,毛管內(nèi)折和毛管端部外表面裂紋等問題,通過采取重新制定合理的加熱參數(shù)、調(diào)整穿孔參數(shù)和改進(jìn)工模具,有效解決了穿孔頂頭損耗大,毛管內(nèi)、外表面質(zhì)量波動(dòng)較大的問題,使頂頭的小時(shí)穿孔支數(shù)達(dá)到125支,平均每個(gè)頂頭的穿孔支數(shù)達(dá)到400支左右,大大提高了生產(chǎn)效率,成本下降顯著。

       

      Abstract: There exist certain problems during the hot-piercing operation for the T91 pipe,including high plug consumption,and occurrence of inner fold and end-outer surface crack of the shell,etc. Accordingly,proper heating parameters and piercing adjustment parameters are determined,while relevant operational tools and dies are modified. As a result,the above mentioned problems concerning high plug consumption and obvious inconsistency of both outer and inner surface quality of the shell are solved,which leads to such a efficiency that the productivity of each individual plug is up to 125 pieces per hour,and the average productivity is about 400 pieces,resulting in considerable enhancement of both the shift output and the cost effectiveness.

       

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